
Is there some trick to this that I'm not aware of...?
I wondered about that, but I've double checked that packages for both the tap and the hurricane nuts, and they both say 10-32.asad137 wrote:No, no trick -- a tap should run easily through a corresponding tapped hole. Are you sure you didn't accidentally get a 10-24 tap instead of a 10-32?
Leland, I think you win the prize this time. I had been trying to spin the tap through the h-nut by just holding the h-nut with my fingers and spinning the tap (with T-handle) through it with my other hand. It got caught every time. However, I just finished trying it on some scrap wood by pulling the h-nut into a 1/4" hole and then tapping it. I met a lot of resistance at first, but I forced the tap through, and, after cutting away quite a bit of material, the tap now goes through without a problem, and the bolt that I could twist through with my fingers before tapping now spins effortlessly through the newly tapped h-nut.LelandCrooks wrote:The taps are much more precise than the bolt or the nuts. Any snag or burr will make it hang. Use a t handle to hold the tap, make sure you're perpendicular, and tap away. Do double check to make sure the tap threads mesh with the bolt.
Personally I'm never using T-nuts, or Hurricane nuts ever again. Once you spin one that hole is a lost cause as far as I concerned. One is enough to ruin a day, sorry to hear about your three. I have a diy alternative idea in mind that will be 100% foolproof for my next project.David Carter wrote:I tried to tap the nuts and spun the first three I tried.
I wish you luck! I wish I had seen this earlier... I spun a hurricane nut in a baffle hole in one of my test runs. I don't think it's a good idea to just reinstall the nut after you stripped out the wood around the shaft... H-nuts bite into the wood and that's part of what holds them in place.David Carter wrote:Not sure if I used enough epoxy, but I think I did. After letting everything sit for 15-20 minutes, I tried to tap the nuts and spun the first three I tried. I have reinstalled the nuts with Gorilla glue to get it to expand around the shaft better than the epoxy. Now I've got to get a better tap. I think I'm going to go ahead and at least trial mount the driver anyway to check hole alignment.
Wish me luck!
Thanks for the additional tips. I used Gorilla glue the second time around on the ones that I spun, and I was able to successfully mount the driver by gradually hand tightening the bolts a little at time. No spun nuts during the trial mounting. I hope it continues to hold up once I'm doing it for real!fender3x wrote:I wish you luck! I wish I had seen this earlier... I spun a hurricane nut in a baffle hole in one of my test runs. I don't think it's a good idea to just reinstall the nut after you stripped out the wood around the shaft... H-nuts bite into the wood and that's part of what holds them in place.David Carter wrote:Not sure if I used enough epoxy, but I think I did. After letting everything sit for 15-20 minutes, I tried to tap the nuts and spun the first three I tried. I have reinstalled the nuts with Gorilla glue to get it to expand around the shaft better than the epoxy. Now I've got to get a better tap. I think I'm going to go ahead and at least trial mount the driver anyway to check hole alignment.
Wish me luck!
Once again, this is a place where dowels came to my aid. In the hole where the h-nut spun, I drilled a 1/2" hole, and put a 1/2" dowel in it, then re-drilled the hole for the h-nut. That way it had a nice, new, snug, hardwood hole for the H-nut to bite into.
Once done drilling, I also sprayed the hole with a fine mist of water, then used Gorilla glue and then let it sit overnight.
This is also the reason that (as I put in some other thread), I tighten the driver down gradually, three turns on each bolt at a time, making several circuits around the driver before it is down tight.
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